Lincoln Navigator Idle and Stall Problems
Got a 1999 navigator w/ 80K miles on it. Just today, it's stalled out 3 times while at stop signs/stoplights. The service engine soon light came on and there's a whining coming from the engine. All fluids are fine. Any ideas?
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This one for example (but only when the engine is cold?).
z72, "Lincoln Navigator Owners: Problems & Solutions" #288, 20 Apr 2006 10:01 pm
Steve, Host
tidester, host
Not wanting to waste a bunch of money chasing a ghost, I have just elected to live with the problem and keep the tank above 1/4 tank.
My 2000 Nav recently had an air ride susp issue with the chk susp light on. The mechanic ran a series of tests to troubleshoot the issue. I saw him playing with the fuses as well as the battery, also, manually pumping air to the air bags via the compressor.......Still have problem BUT the main PROBLEM now is that after all this trial and error, he started the car and the Service Engine Soon light came on, over drive flashing, all lights in the vehicle are on as well. When you drive the vehicle, it stalls..but reverses just fine....Any ideas what could be the problem?.....The only issue I noticed in the past before the suspension problem was that it was idling too high...Please help..I'm desperate ...
Thanks,
Elizabeth
Thanks for your input.
Fergy7
According to what I have read, the fuel pump and regulator appear to be working correctly. Please comment if you see anything wrong with the above test results.
Now I am thinking that there may be water or sludge at the bottom of the tank and when the gas gets low, its getting sucked up or plugging up the fuel pump filter.
My next step will be to make an attempt at siphoning out the gas. Does anyone know if the tank can be siphoned from the filler hose without having to drop the tank?
Anyone have any suggestions?
Thank you,
Fergy7
The gas looked clean, no water or dirt. I filled the tank with 93 octane and thought I may have solved the problem. However, this did not solve the problem either. The truck still hesitates from a stop whenever the tank is 1/4 or lower (cold or hot). Do you think the fuel pressure is dropping below 32 psi when the tank is below 1/4 for some reason?
Unfortunately, I allowed someone to ride in my car who felt the urge to pull upward on the shifter while it was in Drive. The upper part of the shifter separated from the bottom part within the provided connection and I was no longer able to shift at all. The person who did this claims now that it was already broken and that he talked to a Lincoln dealership mechanic who told him it would take a hammer to pull the shifter upward since it is secured. He took the middle console off and finally reattached the top to the bottom part which allowed shifting, but the electronics are now messed up, i.e. the seat heater is not turning off, the cruise is not working.
I watched him pull it up and it came right out, so now I am at a standstill with the repair, the chrome button no longer has resistance and I can shift freely without the security of knowing that the engine is ready to be shifted. He claims that when he "repaired" it 2 screws on the securing plate were missing and that there is some kind of pin or devise that prevents the shifter to be pulled upward. Not only do I now have to deal with this problem on a daily basis, but I am also being belittled by telling me what an idiot I am for thinking that nobody would ever pull up on a shifter knob and if someone did it would be secured by screws. I looked at the mechanism and it appeared to me that when the correct shifting takes place there is a mechanism inside that actually moves upward to move to the next gear, so it really makes no sense that the shifter would be secured downward.
I cleaned the intake and ran fuel injector cleaner through it.
No trouble codes ...but this little flutter in overdrive. Any ideas?
Code reads: O2 sensor signal biased/stuck lean bank 1 sensor 1 and O2 sensor signal biased/stuck lean bank 2 sensor 1.
Symptoms: Rough ideling, stalls, ideling increases and decreases
I have inspected all the vacumn hoses I can see after removing the plastic motor cover and the air filter housing and piping. No obvious problems.
What is most common solution to this fault?