Encoder Motor Problem for 97 GMC Jimmy
Everytime I drive and get on the throttle until I get up to around 40 or 50 miles per hour and then back off the throttle, I begin to hear a whiring noise from the front end, sounds kinda like a drill scoring metal. Anyway, I've changed the control switch on the dash, and had the encoder motor replaced and it still does this when I get on the throttle.
Does anyone have any ideas what exactly the problem might be? My mechanic says that it sounds like the 4-wheel drive is trying to engage at a high speed, however, I'm not sure anymore since I had those things repaired.
Does anyone have any ideas what exactly the problem might be? My mechanic says that it sounds like the 4-wheel drive is trying to engage at a high speed, however, I'm not sure anymore since I had those things repaired.
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A final problem/fix these have is the computer sometimes hangs up so disconncet the battery for 30 minutes and then reconnect and see it the condition clears - it sometimes does.
I mean, I've put in a lot of money to fix this truck. First it was the fuel pump dying on me, and now this. I'm hoping this is the last repair I have to do to this truck.
Also, I'm going to take my truck off of its battery for the half hour you suggested when I return from an errand, but otherwise everything else checked out.
PS: You should be called repairgod.
Disconnecting the battery and reconnecting cleared whatever error condition existed. The 4WD works now, thanks for the advice.
Replaced the four button dash switch, no change. Still blinks and will not drop into 2 wheel, (nor four low) the auto four does stay steady lit. Vacuum switch on the firewall is good. You can here the encoder motor working when I push the buttons, can't say it's engaging...the puzzler is why does it drop out of four high when I pull the fuse?
So by deduction it appears voltage from somewhere is keeping the actuator valve open. When I pull the fuse this of course
cuts the voltage to the actuator valve.
Any suggestions on where to look now?
Parts Repaced: Dash Switch and 4WD Frt Axle Actuator
Current Symptoms:
1. Defaults to 4HI after I switch the ignition on 5 sec off 5 sec then on 10 sec.,will also switch to Auto 4WD.
2. Depressing dash buttons runs 4WD Frt Axle Actuator with whining then vibrating grinding noise at end of cycle. Acts like the actuator is trying to shift gears but overloads, then shuts down when trying to switch to 2Hi or 4Low.
I Checked fuses, left side drivers door and ATV under hood, OK.
Low Fluid level possible ?
Here's the text of the post and the link
http://www.automotiveforums.com/vbulletin/showthread.php?p=4521487#post4521487
EUREKA!!!!!! Found the Problem with the Blazer. After testing all of the components involved with the 4 wheel system I couldn't find any problems...
I finally decided to pull the encoder motor to see if I could shift it manuals to make sure I didn't have a mechanical problem and found the problem. Looking at the encoder motor from underneath It looked almost new. I pulled it off and found a major build up of corrosion between the plastic gasket and the motor gearbox. So much so it distorted the gearbox and bound up the unit so it wouldn't complete the shift. I scraped all the corrosion off and it had a very pronounced bow to the unit. I pulled it all apart ( I'd like to kick the engineer that decided to put security torx bolts in the cover) and separated the 2 halfs. I checked the machined surfaces with a straight edge and found that the housing was warped by at least 3/16th of an inch. I figured nothing ventured nothing gained so I pulled the unit completely apart and using a press straightened the 2 halfs the best I could. I then used a big mill file and flattened the two halfs so they were true. While I had the unit apart i checked the brake unit on the end of the motor and it was fine except that there was some gunk on the friction plate so I cleaned it off. I checked the motor and found one of the stabs for the power feed was almost burnt off. I cleared away some of the insulation and soldered the wires directly to the motor feed wires. No chance to loose continuity again.
I reassembled the unit and installed it back on the transfer case, installed the driveshaft and lowered the truck to check the shift modual connections.
After connecting the modual I replaced the fuses and started the truck. Bingo the truck snapped into 2HI and works like a champ now..
Sorry for the long post but thought you guys would like to have the info.
In shop getting diagnosed tomorrow.
Will let you know what they find.GM junk again.
Kevin
Any suggestions?
Thanks
Thanks
To prevent that from ever happening again I ran a seperate vent for the tranfer case.
I also replaced all of the vac hoses from the transfer case vac switch all the way to the intake manifold. Several sections was already soft from the tranny fluid. I also ran a new line to the vac motor under the battery tray.
thank you all
michael